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Conference Proceedings

The AusIMM Proceedings 1955

Conference Proceedings

The AusIMM Proceedings 1955

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Progress Report on Rod Milling at King Island Scheelite (1947) Limited

The paper gives details of the performance of a 6-ft. by 6-ft. grate discharge ball mill which was converted into a rod mill of the overflow type and then into a grate discharge rod mill. Proposals for further alterations are outlined.INTRODUCTIONThe mill of King Island Scheelite (1947) Limited recovers scheelite by gravity methods.Crushed ore at the rate of 34 tons per hour is divided between two mills. (6 ft. by 6 ft. and 8 ft. by 6 ft. respectively), the mill discharges being pumped to a common distributor which feeds seven Hummer Screens. Each screen has three 4-ft. by 2-ft. Ton-cap sections and repulping compartments are provided. The screen oversize is returned to the mills whilst the screen undersize is finished grinding section product. A third (6 ft. by 6 ft.) mill regrinding the coarser table tailings also discharges into the common Hummer Screen Distributor.The screen undersize is pumped to a bowl classifier which separates at 200 mesh. The bowl classifier sands are treated on tables whilst the bowl classifier overflow, after thickening, is treated in the slime plant by flotation. The flotation concentrate is further concentrated on vanners and slime tables.A recovery of 80 per cent. is possible by tabling whereas only 50 per cent can be recovered in the slime section. The object of comminution is, therefore, to reduce all the new feed to less than a certain mesh (22 mesh Tyler) with the production of a minimum quantity of minus 200 mesh material. cheelite is, a very friable heavy mineral (Sp.Gr. 6'0) and is therefore susceptible to overgrinding. For the evaluation of grinding performance it is hence advisable...
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  • Progress Report on Rod Milling at King Island Scheelite (1947) Limited
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  • Published: 1954
  • PDF Size: 0.15 Mb.
  • Unique ID: P_PROC1955_0779

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